05-02-2008, 08:08 PM
A buddy of mine helped me reinstall the rebuilt C4 back in the Bronco today. Prior to his arrival, I reworked the new torque converter/flexplate adapter.. It was not pulling up tight against the torque converter end face. After it was fixed.. I had 110" of pull back from the converter to the flexplate. I think that should be fine. We ran some Jegs blue hose & 6AN fittings for the new B&M racing cooler. We shall see how well it works. The Art Carr reverse manual shift valve body seems to work fine. It's a real challenge with the Ford/Cummins adapter housing to fasten the flexplate bolts. Thanks Chuck..The folks at Warren Fastenings had what I need. :beer: The complete bottom side of the bell housing to the 4bt Ford/Cummins housing is enclosed. You only have a 1 1/2" hole about half way up the bell housing to install the bolts. (for you Cummins guys it near where your fuel filter is located on your 5.9s..but the hole might not be there on your adapters) All seems to be fine except a small drip from the pan. I guess... I did not straighten the trans pan out well enough around the holes before putting it back to together... I might try to bridge a couple of pan bolts with a strap plate and torque the fasteners again...If that does not work ... I will run it for awhile and dump the transmission fluid and try to fix the leak in the future. When I drove it up & down the street I could see the need for one of those Winters gated shifters!
The little motor has a lot of torque... no problem leaving in 3rd gear from a stop. Of course.. I should not do that very often...
Next....
I have been running a short dump pipe off of the turbo. It is actually not that loud... the turbo really helps to quiet it down. Hope to install the exhaust on Saturday... Should be a major challenge to fab it up... If all goes well then on Sunday I will install the 12 gallon auxiliary tank that BroncoWard sold me..... But I always over estimate what I can get done...cratchhe:
The little motor has a lot of torque... no problem leaving in 3rd gear from a stop. Of course.. I should not do that very often...
Next....
I have been running a short dump pipe off of the turbo. It is actually not that loud... the turbo really helps to quiet it down. Hope to install the exhaust on Saturday... Should be a major challenge to fab it up... If all goes well then on Sunday I will install the 12 gallon auxiliary tank that BroncoWard sold me..... But I always over estimate what I can get done...cratchhe:
'77 EB, 2.5" SL, 2"BL, Cummins 4bt, C4 w/Art Carr manual Valve Body, 35" BFG KM2s
http://www.youtube.com/watch?v=M_HqhiW38ik
http://www.youtube.com/watch?v=M_HqhiW38ik